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build diary << | show individual entries | >>May 11, 2005: Much better looking instruments with the plastic sandwitched between the dash and the gauges. The weekend started off a bit rough. While preparing Janel's Miata for the trip (new springs, shock mounts, exhaust - you know, little stuff) I noticed her supercharger belt was making dust. So I tightened it. That broke on Friday night so Saturday morning was spent putting on a new one. Finally, a couple of hours late, we took off to Utah. The belt broke again about 75 miles later - it seems I have some investigation to do into the superchager. I was happy and unaware of this problem as we zipped down the interstate and then on to the classic 128 into Moab. On the highway, the Seven is remarkably comfortable. The suspension eats up all bumps and undulations. I had earbud headphones on to listen to music so the exhaust noise wasn't bad, and other than high pressure air trying to inflate my left nostril the aerodynamics were good. Without some sort of earplugs the exhaust is loud, though. The new muffler is not as effective as the previous one, particularly at full throttle. On the twisty bits I felt as if we were almost walking although Jeremy and I did get a chance to play for a bit. I also found out that I should not lead a group without a working speedometer, as my estimated 45 mph turned out to be closer to 65. The police officer going the other way merely flickered his lights and gestured for us to slow down. Whew! The event itself was fun. Lots of shiny cars and the new 2006 Miata was in attendance. I crawled all over that one as you might imagine and managed to take some photos with the Seven. The average attendee at the event was older and more interested in cruising and scenery than performance, but once I took the hood off the Seven so they could see the Miata engine I was a little more accepted. In the evening we took a run up to Fisher Towers and a few miles down a rough dirt road. It's a great place for taking photos of cars near sunset and I availed myself of the opportunity to fire off quite a few frames. I also rattled the exhaust pipes free of the collector and popped an exhaust hanger. Not such a good plan and very noisy although it was easy to fix. Jeremy and I then headed for a campsite as Janel went back home due to her brother's graduation. The next day, we were lining up to go on a tour with a group going into the Canyonlands park. I stalled the cold Seven in the parking lot in front of everyone. This got me some teasing about a "poor first impression" - so I decided to give a different one by offering a taste of some tire spin. Nothing major (less than I've used in an autocross start)...but when I was done there was a ticking from the rear end. It sounded like a flange hitting as the differential turned. Uhoh. Nothing was visible so I backed the car up on to some trailer ramps. The diff had shifted a bit and some feeling around indicated that perhaps I'd ripped the diff mount off the frame. With a bit of prying I could drive the car without noise, but the diff was definitely moving up and down. My car lasted longer than any of the other CMC "Miata" frames without this failure but it's my turn now. Lucky for me, Joe Portas (the Knobmeister - if you need custom engraving, shift knobs or other bits talk to him!) was just packing up to head home to Littleton and trailer his Miata. He offered the use of the trailer to get me home to Grand Junction. His wife Mary was quite happy with the arrangement as that meant she got to drive the Miata instead of riding in the tow vehicle. I had a comfy ride home with good company as Joe and I have been seeing each other for years at Miata meets all over the world. It all worked out well. So, what now? The Seven was almost ready for some relatively major work anyhow. I'll put it back up in the air and sort out the differential mount. I'm not sure if I'll do the pseudo-PPF as CMC ended up as I don't think any of those cars have ever actually run. The solution that BSI worked out for the GRM car is tempting and easier to reach. Regardless, the seats are coming out. I'll make a new transmission tunnel cover, add some switches for wipers, fit an electronic speedometer driver, reroute a front brake line, make a better headlight mounting system, add a master power switch and generally do a number of jobs that have been accumulating. I have quite a list. On the way in to Moab for the Miata meet. Since I will have the cover off the transmission tunnel I'm also going to install a new speedometer drive. The 1999 and later Miatas use an electronically driven speedo instead of the cable driven one I have now. The packaging of the transmission is such that the cable has to bend radically shortly after exiting the transmission and the first one lasted 10 miles. A new cable is obviously not the answer so I'll have to see if I can somehow manage to install and drive a later speedo. I've found a junkyard instrument cluster with some damage to the housing, perfect for my intentions. Courtesy of Jeremy Ferber, here's how my Moab trip ended. The failure itself was the mounting bracket on the transmission tunnel. The bolt holding the diff in place was only in contact with a small area of the bracket as this was too far forward. As the diff strained to move up and down, it tore the bracket apart. It's quite possible this was a slow-motion failure that only made itself known after the diff had lifted enough to contact the parking brake. Solutions? I have three options right now. One is to copy what CMC ended up doing and build a tubular version of the PPF. Heikki has some photos of this on his site. It will have to wiggle around the edge of the transmission tunnel and driveshaft flange but it should be possible. It doesn't look compatible with a handbrake, though. One way to make this easier would be to put a plate on the side of the transmission tunnel instead of the tubes. This would open up 3/4" or so of width and I'd probably still be able to work out a way to attach the handbrake. I don't think any cars with this solution have turned a wheel yet although it certainly should work well. Another option would be to copy the solution developed by BSI and used on the GRM car. Again, that car hasn't really been run hard. I'd be concerned with the welded tube coming off the back of the diff but it sure would make life easy. I suspect the weight would be less than the PPF solution as well. The third option would be to simply reinforce the bracket at the nose of the diff. Instead of a thin piece of about 1/8" plate, I'd put in something stronger. It would also be a properly located hole instead of a half-engaged slot. An extra tube would be run straight down from the side of the bracket to ensure it was well supported - possibly a plate. This might be the easiest and lightest solution. Given the amount of abuse my original setup endured I believe this would probably work well - but I do have plans to increase the horsepower of the car at some point. I've also decided to add some stiffer bushings in the side mounts for the diff. They are able to rock back and forth a fair bit. I might also bolt on a piece of C channel to hold the other end of the bolt in place. At the moment it won't move with the diff but that will change with stiffer bushings. The failed differential mount. |