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build diary << | show individual entries | >>May 16, 2005: Since I will have the cover off the transmission tunnel I'm also going to install a new speedometer drive. The 1999 and later Miatas use an electronically driven speedo instead of the cable driven one I have now. The packaging of the transmission is such that the cable has to bend radically shortly after exiting the transmission and the first one lasted 10 miles. A new cable is obviously not the answer so I'll have to see if I can somehow manage to install and drive a later speedo. I've found a junkyard instrument cluster with some damage to the housing, perfect for my intentions. Courtesy of Jeremy Ferber, here's how my Moab trip ended. The failure itself was the mounting bracket on the transmission tunnel. The bolt holding the diff in place was only in contact with a small area of the bracket as this was too far forward. As the diff strained to move up and down, it tore the bracket apart. It's quite possible this was a slow-motion failure that only made itself known after the diff had lifted enough to contact the parking brake. Solutions? I have three options right now. One is to copy what CMC ended up doing and build a tubular version of the PPF. Heikki has some photos of this on his site. It will have to wiggle around the edge of the transmission tunnel and driveshaft flange but it should be possible. It doesn't look compatible with a handbrake, though. One way to make this easier would be to put a plate on the side of the transmission tunnel instead of the tubes. This would open up 3/4" or so of width and I'd probably still be able to work out a way to attach the handbrake. I don't think any cars with this solution have turned a wheel yet although it certainly should work well. Another option would be to copy the solution developed by BSI and used on the GRM car. Again, that car hasn't really been run hard. I'd be concerned with the welded tube coming off the back of the diff but it sure would make life easy. I suspect the weight would be less than the PPF solution as well. The third option would be to simply reinforce the bracket at the nose of the diff. Instead of a thin piece of about 1/8" plate, I'd put in something stronger. It would also be a properly located hole instead of a half-engaged slot. An extra tube would be run straight down from the side of the bracket to ensure it was well supported - possibly a plate. This might be the easiest and lightest solution. Given the amount of abuse my original setup endured I believe this would probably work well - but I do have plans to increase the horsepower of the car at some point. I've also decided to add some stiffer bushings in the side mounts for the diff. They are able to rock back and forth a fair bit. I might also bolt on a piece of C channel to hold the other end of the bolt in place. At the moment it won't move with the diff but that will change with stiffer bushings. The failed differential mount.
On the Seven front, I've obtained an instrument cluster from a 2001 Miata so I can use the electronic speedometer and replace my broken cable. This should be an interesting swap but I'll make it work. Somehow. The differential will get some attention shortly. I'll pull the rear bulkhead apart this weekend and come up with a final solution. While the transmission is uncovered, I'm going to see if I can replace my mechanically driven speedometer (well, it would be mechanically driven if the cable would stop snapping) with this electrically driven one from a 2001 Miata. The procrastination isn't complete, however. I pulled the scuttle and rear bulkhead off this past weekend. It's almost shocking how quickly I can disassemble this car and make it look unfinished. Removing the rear panel uncovered the bracing that's available back there. There's a lot of strength, more than enough to keep the diff tied down if the bracket itself is strong enough. I'll probably just build a stronger mount for the nose. The diff will have to come out in order for me to put new bushings in the side "arms", though. That's going to be a hassle as I have to wrestle with a 75 lb chunk of metal that is a tight fit into the frame. Oh well, if it was easy everyone would be doing it. The scuttle was removed to give access to some of the wiring and the speedometer drive. The mechanical one has been removed and will be replaced with an electric one. Luckily, the gearing of the unit is the same as my car so it should be accurate. The hard part will be fitting the speedometer in the earlier housing. Well, not that hard. Again, if it was easy... The mechanical and electronic speedometer drives. |